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ATHOL-ROYALSTON PROJECT DESCRIPTION & SUMMARY White Paper February 2002 Prepared by: Rob Rizzo, Associate Director ABSTRACT: In 1998 the Athol-Royalston Regional School District installed a wood
chip heating system in the Athol High School to replace/supplement
an aging fuel oil system. This report summarizes the data from their
first three heating seasons during which the School District realized
an estimated savings of over $26,000.00 through the utilization of
a biomass heating system. PROJECT
DESCRIPTION:
PROJECT
COSTS:
EQUIPMENT
DESCRIPTION: The wood chip equipment is comprised of a number of elements to establish a complete, automatic operating system:
In the original design, the
planned capacity of the fuel storage system was limited to 20 tons (approximately
one trailer load) of chips. This resulted in problems with truck delivery
scheduling. At times the system had to be shut down resulting in burning
more fuel oil than anticipated. During the summer of 2001, the staff
has resolved this problem by increasing total capacity to approximately
30 tons. The School District purchased a complete turnkey package from CHIPTECH Corporation of South Burlington, VT. Included were:
The existing
chimney did not need replacement FUEL
SOURCE & SPECIFICATIONS:
ANNUAL
FUEL CONSUMPTION: Prior to the conversion,
the High School burned fuel oil with no emission controls in place. TABLE 1. ANNUAL FUEL CONSUMPTION (prior to conversion to wood)
At the end of the 1996 -1997 heating season, the District chose to use the lighter, more refined #2 heating oil to 'extend the life' of the aging oil burner. TABLE 2. ANNUAL FUEL CONSUMPTION and COST SAVINGS SINCE CONVERSION
Table 2 illustrates that during the 2000-2001 heating season a number of changes occurred to contribute to a 58% increase in annual savings over the previous year. During this heating season, the school switched from burning whole tree chips to sawmill residue chips. It should be noted that although sawmill chips cost 60% more/ton than whole tree chips, the efficiency and BTU value output increased by 28% due to a lower MC of the sawmill chip. In addition, the consumption of 72% more chips than the previous year greatly increased the total annual savings. As mentioned earlier, whole tree chips are less consistent in size and quality than sawmill residue chips. At times, the chip feed system would become clogged at the out-feed of the storage bin due to an over-sized branch, twig, a piece of bark, or wood becoming jammed and stopping the flow of the feed stock. This resulted in the wood system shutting down and the back-up oil system starting up. The automatic switching by the system to fuel oil contributed to the overuse of fuel oil for the first two years of operation. School maintenance personnel retrofitted the out-feed of the storage bin at the end of the second season, which they believe ended their clogging problem. A more likely scenario is that the change from whole tree chips to sawmill residue chips remedied the problem. It is unknown if the manufacturer is aware of this chip-handling problem, or if it has been a problem in other applications. Future purchasers may wish to consider alternative designs, using whole tree chips that have been screened to remove over-sized pieces, or working with the manufacturer to remedy this potential problem. Total Savings
to the School District from first three years of operation: $26,535.66 Annual Savings have been calculated as follows:
1998-1999 heating season: 52,703 gallons x $.54/gallon
= $28,459.62 (assumed total fuel cost without 1999-2000 heating season: 52,703 gallons x $.63/gallon
= $33,202.89 (assumed total fuel cost without conversion) 2000-2001 heating season: 52,703 gallons x $.89/gallon
= $46,905.67 (assumed total fuel cost without conversion) $8,431.42
+ $7,018.47 + $11,085.77 = $26,535.66 Total Savings Contracts have been executed for the 2001 -2002
heating season: The District purchased whole tree chips from a local land clearing company for the first two years of operation. It was decided to purchase debarked, hardwood sawmill residue chips from local sawmills at the start of the third-heating season. This was done primarily to obtain:
Table 3. Differing heat values based upon average MC
A science class at the High School analyzes each load of chips for MC as a component of the curriculum. During the 2000-2001 heating season, the sawmill residue chips averaged 28% MC. As illustrated in Table 3, this is not typical of hardwood chips in the Northeast. Possible reasons for the lower MC might include; incorrect laboratory analysis or calculation of MC, a wide variety of species, or delivery of chips from logs that were not freshly cut. CONCLUSION: The annual savings to the
District in the third year of operation (2000-2001) is significant. A
reduction of over 10,000 gallons of #2 fuel oil from the previous year,
and an overall reduction of over 31,000 gallons per year as compared
to the fuel oil usage before the conversion demonstrates that the District
is saving money. In fact, in the first three years of operation the
conversion has saved $26,535.66 and has offset 76,745 gallons of #2 fuel
oil. The Athol High School wood
chip heating system is saving the School District money over the fuel
oil system that it has replaced. This system is capable of greater savings
as has been documented in case studies in Vermont where over 20 schools
have installed wood chip heating systems. Further investigation is recommended
to examine some of the interacting components of the system such as the
efficiency and cycling of the back-up oil burner, the electrical controls
to analyze how the wood boiler interacts with the back-up burner, the
electrical engineering design, the heat exchange system, the ventilation
control strategies, and the stack temperature. The above should be components
of a complete energy audit performed at the school to ensure that the
system is at the maximum efficiency. Other Energy Conservation Measures
(ECM's) should be examined to further reduce the heating load and increase
the climate control efficiency of the school building. The local electricity
utility company has professionals on staff to assist in this regard. This report has not attempted
to calculate the total impact on the local economy, but it should be
noted that Hubbard Forest Industries, Inc. of Royalston MA has been supplying
the sawmill wood chip residue fuel, and the Royal Steam Heater Co, Inc.
of Gardner MA completed the installation. Every heating system will perform differently based upon the interacting components mentioned above, other ECM's that have been employed, and the fuel source and consistency. These factors must be taken into consideration in the planning and engineering of a new or replacement system. This report has attempted to summarize the Athol biomass conversion project based upon the facts presented by school personnel. CONTACTS: Rob Rizzo, Associate Director Special thanks to Bob Muzzy,
Maintenance Operations Supervisor, Athol-Royalston Regional School District,
250 S. Main St., Athol, MA 01331; 978-249-2400; and Tim Maker, Director, Biomass Energy Resource Center, P.O. Box 1611, Montpelier, Vermont, 05601. Tim can be reached at 802-223-7770 or fax 802-223-7772
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